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Get your copy of "MPC performed multiple cuts under compression in a single operation, saved 24 hours rig time"

An operator with a 30-year old well in the
Marat formation in West Kuwait wanted
to recover as much tubing as possible in
order to have the lowest kickoff point for
sidetracking a producing formation. The
operator tried to set a whipstock at 13,300 ft
(4054 m), but it failed because the string was
stuck and the completion assembly couldn’t
be pulled out. The completion string was
completely stuck due to the accumulation
of barite in the annulus between the tubing
and the coal seam gas. MPC-Saved-24-Hours-Rig-Time-Marat-Kuwait-cs.pdf