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xSight™ smart intervention optimization service were used for a high-risk deepwater Gulf of Mexico workover project. The objective was to remove a retrievable high-pressure/ high-temperature isolation packer set at 26,254 ft (8,002 m) measured depth (MD) to allow the operator to abandon and recomplete the well above a failed gravel pack.

The operator used the downhole data acquisition tools to measure the force being applied to the fish in real time. This was a major concern since the extreme depth and well profile meant that surface gauges would be inaccurate. On the first run—to retrieve the seal assembly and anchor latch—the benefit of xSight real-time measurements was highlighted immediately. Upon tagging up on the seal assembly, the downhole real-time data measured more than 40,000 lb (18,144 kg) of force being applied on the fish before the surface gauge indicated the seal assembly was engaged. Without these readings, the rig would have continued to set down weight and could have easily damaged the weaker 2 3/8-in. regular connection used in the fishing bottom hole assembly (BHA).

After identifying the large discrepancy, the operating team, including xSight engineers, used real-time xSight service readings as the primary verification instrument and the other gauges as a backup. They verified that the seal assembly was engaged with the type “D” spear and rotated the seal assembly under tension 12 to 13 rounds to release the anchor latch. At surface, it took more than 24 full rotations before the downhole sensors measured any torque going through the BHA to the seals. At exactly 36 rounds at surface, the torque fell off to zero while the tension reading dropped sharply and measured a tension of ~300 lb (136 kg) force still acting on the toolstring. This additional weight was due to the seal assembly (expected weight was 275 lb [125 kg] downhole) hanging from the spear. The additional weight confirmed the seal assembly had been released correctly and verified the successful retrieval before pulling out of hole.

Download the PDF to read the full case study.


Challenges & Results


  • Fish a lightweight seal assembly and isolation packer from a depth of 26,254 ft
  • Use a small 23 /8-in. connection on top of a spear on the fishing BHA to retrieve the fish through an S-curved well with a tangent section with a hole angle greater than 70°


  • Identified significant weight/force discrepancies between surface and downhole
  • Identified successful retrieval of seal assembly in real time
  • Identified successful retrieval of isolation packer in real time before pulling out of hole